Okay, so here's my problem...
For the most part, the quad flies great, the only time it oscillates is when I'm trying to descend. This was the first time it had ever oscillated out of control during descent that resulted in a crash though. Today, after piecing it back together, I went to go see if I could recreate the (1:09) death wobble by rocking the controls back and forth. Sure enough, if I moved them quick enough. it would start uncontrollably oscillating back and worth till it crashed to the ground.
Any ideas?
Setup:
- HK KKboard v2.1 running XCopter 4.7
- Turnigy Plush 12a
- 25.2x26mm 2200kv Brushless Outrunner
- 2s 1800mAh